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借助OM、激光共聚焦显微镜、质谱仪和电解萃取等设备和方法,研究了添加微量稀土La(质量分数0.001 1%)的取向硅钢在轧制前采用不同加热保温时间对抑制剂固溶行为的影响。结果表明:当稀土取向硅钢在1 250℃分别保温10、20、30 min后,试验钢晶粒尺寸随保温时间延长有先快后慢的长大趋势;三种抑制剂元素Mn、Cu和Al均发生固溶,保温时间对Mn和Cu两种元素的固溶影响明显,固溶量分别由69.8%和43.7%增加至84.2%和85.2%;随着保温时间的延长,稀土取向硅钢中抑制剂的小尺寸未溶物逐渐减少直至消失,较大尺寸未溶物(300~600 nm)逐渐转变为小尺寸未溶物逐步溶入基体中,数量减少且未溶物的类型由复杂逐渐转变为单一。 In this paper the solid solution behavior of the inhibitor under various holding time in 0.001 1 %La oriented silicon steel during reheating had been investigated by using OM, LM, methods of electrolytic extraction and mass spectrometer. The results showed that grain size of the test steel increased significantly with the holding time prolonging when the rare earth oriented silicon steel was heated to1 250 ℃ and held for 10, 20 min and 30 min respectively, and the growth trend slowed down after ... 
2022-02-28 174 5.8

本实用新型公开了一种防溢出的无取向硅钢绝缘涂液存储装置,涉及无取向硅钢绝缘涂液技术领域,为解决现有无取向硅钢绝缘涂液存储设备在存储过程中存在涂液过满,导致液体溢出产生浪费现象的问题。所述绝缘涂液存储机构本体上方的一侧设置有液位监测器,所述液位监测器的下端设置有监测杆,所述液位监测器的输出端设置有单片机,且液位监测器的输出端与单片机电性连接,所述绝缘涂液存储机构本体的内壁设置有压力传感器,且压力传感器设置有若干个,所述压力传感器的输出端与单片机的输入端电性连接,所述绝缘涂液存储机构本体的内部设置有泵体,且泵体设置有两个,所述泵体的一端设置有溢流输送管。
2021-09-02 166 6.8

利用EBSD技术研究了电工钢中长轴平行于轧向的柱状晶样品在热轧和退火过程中组织和取向的演变规律,并与长轴平行于板法向的样品的已有研究结果进行对比。结果表明,无论柱状晶按何种方向排列,只要表面存在剪切力,热轧后都可形成剪切织构,同时中心形成轧制织构,主要包括旋转立方织构和{112}<1-10>。柱状晶造成的影响主要体现在板中心层,长轴平行于轧向排列的样品热轧时形成的粗大旋转立方晶粒要到脱碳退火后才能完全消除,但破坏了正常的不同取向晶粒间的取向差分布及尺寸均匀性,导致二次再结晶不完全及磁性能降低。 The evolution of microstructure and grain orientation in an electrical steel containing columnar grains with its long axis being parallel to the rolling direction of sheet was studied during hot rolling and annealing by EBSD technique.The results are compared with those of samples containing columnar grains being parallel to normal direction of sheet reported in the reference [3].It was shown that,whether the long axis of columnar grains was arranged in RD or ND,shear textures can be formed in t... 
2011-02-28 181 5.8

为了解决目前冷轧产线硅钢现有切边技术存在的微裂纹、应力、毛刺和边浪等问题,采用光纤激光器进行了高速切割实验,对激光功率、切割速度、激光模式等影响因素进行了分析,同时对高速切割时的切割前沿形状进行了研究。结果表明,切割最高速度随着功率的增加而增加;随着离焦量的增加,切割质量下降,挂渣增多,切缝宽度增加,切割深度变浅;基模激光器能量密度更高,所以薄板切割时的切割速度高于多模激光器;切割前沿随着切割速度的增加会变得平缓,速度足够大时,切割前沿甚至接近与切割方向平行,此时切缝下部存在挂渣现象。 In order to solve the problems such as micro crack,stress,burr,edge waves and so on,existing in cold rolling production line of silicon steel side cutting,experimentsof high speed laser cutting using fiber laser were carried out.Laser power,cutting speed,laser mode and other factors were analyzed,at the same time,cutting front geometries were studied.The results show that the maximum speed increases with power.And the increases of defocus result in poor quality,wider kerf and shallowerkerf.Energ... 
2013-04-28 119 5.8

利用OM、TEM与EDS技术,对Fe-3.2%Si低温取向硅钢热轧板进行不同常化冷却工艺处理后的显微组织、析出相及最终产品的磁性能进行分析,并与热轧板的组织和析出相进行对比。结果表明,常化板较热轧板的表层组织均匀,基体中再结晶比例增加,带状组织变窄;常化板中析出物的数量明显比热轧板的多,析出物主要有AlN、MnS及复合析出的(Cu,Mn)S等。在常化温度1120℃、保温3 min的条件下,采用二段式冷却较空冷、淬沸水、淬常温水的冷却工艺,常化板表层显微组织更均匀,沿板厚方向的显微组织的不均匀性显著,取向硅钢的磁性能最高;常化后采用二段式冷却工艺析出的细小析出物数量最多,且弥散分布在基体中,抑制剂的抑制效果最好,对成品获得高磁性最有利。 Microstructure, precipitate and magnetic characteristic of final products with different normalizing cooling processes for Fe-3.2%Si low-temperature hot-rolled grain-oriented silicon steel were analyzed and compared with the hot-rolled plate by optical microscopy(OM), transmission electron microscopy(TEM), and energy dispersive spectrometry(EDS). The results show that, the surface microstructure is uniform, the proportion of recrystallization in matrix increases, and the banding textures are nar... 
2014-03-28 172 5.8

以不断增长的薄板坯流程为背景,与传统流程对比分析了薄板坯流程无取向电工钢热轧晶粒组织特征;以50W800和50W1300钢为典型实例,探讨了两种流程下成品板晶粒组织、织构、磁性能及其磁时效行为的基体差异和相关原理。研究表明,薄板坯流程热轧板组织较粗大,有利于在成品板中获得粗大的晶粒和有利的织构,从而得到较低的铁损和较高的磁感。然而,薄板坯流程会造成第二相粒子的细小弥散分布与不充分析出,容易因磁时效而使磁性能恶化。 Based on the rapid development of compact strip production(CSP) processing,the characteristics of hot band grain structure produced by CSP processing were analyzed in comparison with those of conventional technology.The basic differences in grain size,texture,magnetic properties and the magnetic aging behaviors of the final sheet products produced by the two processing technologies and the corresponding principles were discussed,while steel 50W800 and 50W1300 were taken as examples.It is indicat... 
2013-04-28 155 5.8

冷轧中中低牌号的无取向硅钢多采用万能凸度轧机(Universal crown mill,UCM)生产,其板形好坏受制于UCM轧机板形调节手段的协调使用。为掌握UCM轧机的板形控制特点,建立基于二维变厚度有限元的辊系弹性变形和基于三维差分的轧件塑性变形的六辊轧机耦合模型,对UCM轧机的板形调控性能进行详尽的分析,包括工作辊和中间辊弯辊、中间辊窜辊的调控功效、辊间接触压力分布等。在此基础上,提出可用指导生产的板形控制策略,指出UCM轧机在横向厚差控制方面的不足。针对工业生产中UCM轧机轧制无取向硅钢横向厚差大的问题,在大量仿真计算的基础上,开发具有高次曲线函数的边部变凸度(Edge variable crown,EVC)的工作辊。采用该工作辊后,各种品种的无取向硅钢的横向厚差不大于10μm的百分比由24%提高到99%,横向厚差的均值小于6μm,远小于之前的13μm。 Medium-low grade non-oriented silicon steel is rolled often by universal crown mill(UCM) during cold rolling.Its shape quality is dependent on the coordinated control of several shape adjustment devices of UCM.In order to understand the shape control characteristics of UCM,coupling model of six-high rolling mill,based on two-dimensional varying thickness finite element rolls elastic deformation model and three-dimensional finite difference strip plastic deformation model,is setup for the detaile... 
2011-10-28 158 5.8

介绍了电工钢生产线连退机组的表面处理工艺,特别是电解清洗系统的工作机理、设备构造、生产工艺及各种影响因素。 This paper introduces the technology of surface treatment of continuous annealing unit in electrical steel production line,in particular the working mechanism,structure of equipment,production techniques and various influence factors of the electrolytic cleaning system. 
2023-05-11 1.34k 5.8

采用硅钢自动测量装置及X射线衍射仪检测出样品在实验前后的磁性能参数和织构强度.结果表明:较低的电压、9 Hz、较长的处理时间以及退火温度为650℃有利于增高铁损降低比例;较低的电压、较高的频率以及退火温度为650℃有利于增加磁感应强度增高比例.最佳的提高磁性能的实验参数是:频率为9 Hz,电压为500 V,处理时间为6 min,退火温度为650℃.通过织构分析可以验证:取向硅钢磁感应强度的变化取决于{110}<001>晶粒取向度值,而{110}<001>取向度值可看成是一个反映总体平均偏离角大小情况的综合值. An automatic measurement system for silicon steel and an X-ray diffraction meter were used for measuring the magnetic property parameters and texture of ex-processed samples and processed samples.It is shown that under the condition of a lower voltage,9Hz,a longer processed time and an annealing temperature of 650℃,the decrease rate of iron loss can be increased;a lower voltage,a higher frequency and an annealing temperature of 650℃ are in favor of improving the increase rate of magnetic inducti... 
2011-08-28 145 5.8

【作者】 朱凤泉; 黄生银; ...
2013-01-28 163 5.8

采用RH精炼添加钙合金方式对硅钢进行钙处理。结果表明,钙合金添加量为0.67、1.00、1.67kg/t钢时,钢中钙含量分别为0、2×10-6、4×10-6;随着钙合金添加量增大,钢中夹杂物粒度逐渐由0~2μm向2~4、4~6μm偏移;不同钙处理条件下,钢中均存在粒径小于1μm和粒径为1~5μm的MnS、CuxS夹杂物,后者或单独存在,或同AlN、CaS夹杂复合;粒径为5~10μm区间,钢中的夹杂物基本以钙的氧、硫化物为主。与钙处理前相比,钙合金添加量为0.67、1.00、1.67kg/t钢时,粒径小于1.0μm的微细夹杂物减少幅度分别为68.06%、87.50%、94.94%。钙合金添加量为1.67kg/t钢时,可以去除钢中绝大部分的微细夹杂物。 Ca alloy was added into the liquid steel during RH refining,and the results show that Ca concentration in final Si steel sheets is insignificant,about 0,2×10-6 and 4×10-6 when the added amount of Ca is 0.67,1.00 and 1.67 kg/t steel,respectively.With the increase in the added Ca alloy amount,the inclusions in the steel gradually change from those of 0~2 μm to those of 2~4 and 4~6 μm.Under different Ca treatments,there exist MnS and CuxS inclusions whose size is below 1 μm as well as MnS and CuxS ... 
2013-02-28 152 5.8

【作者】 姚昌国; ...
2011-05-28 151 5.8

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