所有分类
  • 所有分类
  • 未分类

本发明属于钢铁冶炼技术领域,涉及一种超低铝极低硫无取向硅钢的冶炼方法,包括如下步骤:KR铁水预处理→BOF复吹转炉冶炼→RH真空炉精炼→LF精炼→连铸;采用本发明中的冶炼方法,铁水脱后硫可以适当放宽,转炉出钢温度可以适当降低,RH工序无需采用OB法升温,也无需RH顶枪喷粉或者加入合成渣脱硫,LF只需实现微调成分、调节温度、平衡炉机节奏以及适当脱硫。此种冶炼方法充分利用并发挥了各工序优势,避免了在某一工序完成所有冶炼任务,一旦发生事故,容易造成生产中断,产品质量难以保证。
2021-09-24 148 6.8

一种硅钢变压器绕线模具,包括模具本体、顶梁、举升梁、螺杆、绕盘,其特征在于顶梁设置在模具本体的顶部,举升梁设置在模具本体的下端,模具本体的顶端设有螺丝杆,顶梁穿过螺丝杆通过活动螺母固定,模具本体的中部设有镂空,螺杆转动设置在镂空中,螺杆穿过模具本体下端与绕盘连接,模具本体的中部设有至少两个连接梁,举升梁在连接梁中穿过移动,并且中部穿过螺杆,模具本体的底部设有槽体,模具本体的中部连接梁与槽体底部链接,举升梁移动到最低点时设置在槽体内,本方案通过螺杆和绕盘以及举升梁的相互作用将线圈通过机械能作用顶出模具,省去了人为的力量。
2021-04-16 121 6.8

本实用新型公开了一种硅钢片生产用冲压模具,包括承重板,所述承重板的上表面分别设置有缓冲机构和安装架,缓冲机构包括固定连接在承重板上表面的缓冲座,缓冲座的上表面开设有升降腔,升降腔的内部竖向滑动连接有冲压母模,冲压母模上边沿的下表面固定连接有缓冲弹簧,缓冲弹簧的底端与升降腔的内底壁固定连接,冲压母模的内底壁设置有气压顶出机构。该硅钢片生产用冲压模具,在合模过程中,冲压母模能够在缓冲弹簧的作用下沿升降腔缓慢下降,对合模的冲击力进行缓冲,从而达到对整体结构进行保护的目的,在冲压母模停止下降后,合模操作完成,随后液压杆带动冲压公模上升,冲压母模在缓冲弹簧的弹力作用下复位,便于下次冲压加工操作的进行。
2021-10-15 137 6.8

采用RH精炼添加钙合金方式对硅钢进行钙处理。结果表明,钙合金添加量为0.67、1.00、1.67kg/t钢时,钢中钙含量分别为0、2×10-6、4×10-6;随着钙合金添加量增大,钢中夹杂物粒度逐渐由0~2μm向2~4、4~6μm偏移;不同钙处理条件下,钢中均存在粒径小于1μm和粒径为1~5μm的MnS、CuxS夹杂物,后者或单独存在,或同AlN、CaS夹杂复合;粒径为5~10μm区间,钢中的夹杂物基本以钙的氧、硫化物为主。与钙处理前相比,钙合金添加量为0.67、1.00、1.67kg/t钢时,粒径小于1.0μm的微细夹杂物减少幅度分别为68.06%、87.50%、94.94%。钙合金添加量为1.67kg/t钢时,可以去除钢中绝大部分的微细夹杂物。 Ca alloy was added into the liquid steel during RH refining,and the results show that Ca concentration in final Si steel sheets is insignificant,about 0,2×10-6 and 4×10-6 when the added amount of Ca is 0.67,1.00 and 1.67 kg/t steel,respectively.With the increase in the added Ca alloy amount,the inclusions in the steel gradually change from those of 0~2 μm to those of 2~4 and 4~6 μm.Under different Ca treatments,there exist MnS and CuxS inclusions whose size is below 1 μm as well as MnS and CuxS ... 
2013-02-28 136 5.8

采用双辊连铸工艺制备了硅的质量分数分别为0.5%,1.0%,3.0%,4.5%的硅钢薄带,用光学显微镜观察其组织,并研究了后处理工艺对薄带组织和性能的影响。结果表明:硅含量为0.5%和1.0%的薄带适合采用一次冷轧+850~950℃退火的后处理工艺,而硅含量在3.0%以上的薄带适合采用二次冷轧+950℃退火的后处理工艺;硅含量为3.0%和4.5%的薄带在冷轧并950℃退火后,其磁性能最佳,铁芯损耗约为4.30 W·kg-1,磁感应强度约为1.68T。 Silicon steel thin strips with silicon content of 0.5wt%,1.0wt%,3.0wt%and 4.5wt%were prepared by twin-roll continuous casting process,and the microstructure of the strips were observed by means of optical microscopy,and on the basis,the effect of post-treatment process on microstructure and properties of the strips was studied.The results show that the post-treatment process of one-time cold rolling and annealing between 850—950℃was suitable for the strips with silicon content of 0.5wt%and 1.0wt... 
2011-08-28 126 5.8

本实用新型涉及变压器材料检测技术领域,具体为一种硅钢片检测装置,包括材料检测装置主体,材料检测装置主体包括相互连接的铁损测试仪主机及磁导计,磁导计的顶端设置有清洁机构,清洁机构包括固定盒、拉块及刷块,固定盒固接于磁导计上,拉块插设于固定盒中、能够在固定盒中上下移动,固定盒的内部底面上及拉块的底端上分别安装有刷块,铁损测试仪主机上还设有束线机构。本实用新型使得用户可在检测硅钢片前,对硅钢片两面沾染的灰尘污渍进行擦拭,避免灰尘污渍影响对硅钢片的测定结果,可方便地对刷块进行清洁更换,使得用户可方便地对电源线和导线进行收纳。
2021-08-16 118 6.8

针对采用含钒铁水生产无取向电工钢存在的铁水脱硫率低、转炉冶炼过程回硫量大、成品硫含量偏高的问题,通过对含钒钛铁水脱硫,减少转炉冶炼过程回硫以及RH脱硫技术等方面的研究,大幅度降低了电工钢成品硫含量。生产表明钢中w(S)=0.001 9%~0.006 9%,平均为0.004 2%;w(S)≤0.008%的比例达到了100%,且w(S)≤0.005%的比例也达到了91.43%。 In cognizance of the problems of low desulphurization rate for hot metal,large sulfur-recovery in converter as well as high sulfur content in products in producing non-orientation electrical steel with vanadium-content hot metal countermeasures have been carried out.Sulfur content in non-orientation electrical steel is decreased obviously by way of study on technologies of desulphurization for hot metal with vanadium & titanium,sulfur-recovery control in converter and desulphurization in RH ... 
2013-01-28 127 5.8

针对某硅钢车间ST机组的除尘系统除尘效率较低、排放浓度不达标、二次污染较严重的问题,通过现场调研,对除尘系统、含尘气体组分与物性参数等进行测试和分析,运用管道伴热技术改善粉尘黏性后,再选取合适的除尘器对粉尘进行除尘处理,大大地提高了系统的除尘效率。 To solve the problems of low dust removal efficiency, substandard emission concentration and severe secondary pollution, some investigations are conducted to test and analyze the dust removal system,dust-gas composition and relevant physical parameters.Moreover, dust removal efficiency is greatly improved by the use of pipe heat tracing technology and by choosing appropriate dust remover. 
2014-02-28 109 5.8

本实用新型涉及一种硅钢卷用放料架,属于硅钢卷放料技术领域。包括底板、升降台、支撑座、旋转座、固定轴、内限位块、轴套和外挡块,所述底板上设有升降台,升降台上设有支撑座,支撑座上设有旋转座,旋转座上对称设有两组固定轴,所述固定轴内侧固定有内限位块,其外侧设有可拆卸的外挡块,所述轴套安装在内限位块和外挡块之间的固定轴上且可相对固定轴转动;本实用新型采用升降台,方便人工将笨重的硅钢卷轻松的装入固定轴上,通过可拆卸的外挡块固定,安装快捷,节省人力,安全可靠。
2021-06-15 135 6.8

利用EBSD技术研究了电工钢中长轴平行于轧向的柱状晶样品在热轧和退火过程中组织和取向的演变规律,并与长轴平行于板法向的样品的已有研究结果进行对比。结果表明,无论柱状晶按何种方向排列,只要表面存在剪切力,热轧后都可形成剪切织构,同时中心形成轧制织构,主要包括旋转立方织构和{112}<1-10>。柱状晶造成的影响主要体现在板中心层,长轴平行于轧向排列的样品热轧时形成的粗大旋转立方晶粒要到脱碳退火后才能完全消除,但破坏了正常的不同取向晶粒间的取向差分布及尺寸均匀性,导致二次再结晶不完全及磁性能降低。 The evolution of microstructure and grain orientation in an electrical steel containing columnar grains with its long axis being parallel to the rolling direction of sheet was studied during hot rolling and annealing by EBSD technique.The results are compared with those of samples containing columnar grains being parallel to normal direction of sheet reported in the reference [3].It was shown that,whether the long axis of columnar grains was arranged in RD or ND,shear textures can be formed in t... 
2011-02-28 161 5.8

采用固溶强化、细晶强化和位错强化方法,模拟TSCR流程试开发高强度无取向电工钢,试开发钢的主要合金成分为3%Si、0.83%Al和2.99%Mn。分析热轧、常化、退火后的钢板组织,并针对不同的成品板组织,详尽地分析了相应的力学性能和磁性能。试验电工钢平均晶粒直径为12.37μm时,R p0.2为530 MPa,R m为618 MPa;当退火制度为700℃×4 min,成品组织完全为未再结晶的回复组织时,R p0.2为853.5 MPa,R m为895.5 MPa。该成分的电工钢P15/50或P10/400最小时,对应的平均晶粒直径都大于59.67μm;P10/800或P10/1000最小时,对应的平均晶粒直径都处于12.37~59.67μm尺寸区间。 TSCR was simulated to develop high-strength non-oriented electrical steel with 3% of Si,0.83% of Al and 2.99% of Mn by solution strengthening,grain refinement strengthening and dislocation strengthening.The microstructures of hot rolled plates,normalized plates and annealed plates were analyzed.Furthermore,the mechanical properties and magnetic properties of products with different microstructures were detailedly studied.As the average grain diameter of the steel was 12.37 μm,the yield strength ... 
2013-04-28 151 5.8

为提高无取向硅钢导磁性能,研究了不同剪切方式对无取向硅钢剪切处磁畴结构的影响。利用纳米磁流体观测无取向硅钢剪切后边部磁畴结构。结果表明,硅钢无论在机械剪切还是线切割后的边部磁畴都会发生不同程度的改变:线切割对边部磁畴结构改变较小,边部磁畴分布均匀且连续,在距边缘0~20μm范围内出现磁畴宽度变小现象;机械剪切对磁畴的改变较为严重,剪切处磁畴零乱且不连续,在距边缘20μm处仍难以观察到完整的磁畴结构。 The effects of different shearing modes on magnetic domain structure of cold rolled non-oriented silicon steel are studied in this paper.The magnetic domain of cold rolled non-oriented silicon steel is observed by nanometer magnetic fluid pattern method.The results show that the edge magnetic domain structure will be changed by mechanical shear and wire-electrode cutting,the variation of edge magnetic domain structure wire-electrode cutting edge is very small,the magnetic domain structure is wel... 
2012-04-28 133 5.8

站点公告

网站试运行,请大家关注本站公众号,多提宝贵意见!

显示验证码
没有账号?注册  忘记密码?