钢厂
CN202111247576.4一种冷轧硅钢厚度缺陷识别方法、装置及系统
本发明涉及一种冷轧硅钢厚度缺陷识别方法、装置及系统,本发明的方法包括如下步骤:采集带钢设定厚度及其实际测量厚度并保存;将带钢实际测量厚度与带钢设定厚度相减得到实时厚度差;根据实时厚度差计算厚度缺陷评分;根据评分结果,确定带钢在厚度这一指标的缺陷等级。本发明评估过程考虑了厚度波动情况,并进行量化,能成功识别冷轧硅钢的厚度缺陷,设别准确性较高,提高了冷轧硅钢生产水平,为冷轧硅钢质量控制提供依据。
6.5%Si高硅钢铸锭凝固组织的CAFE法模拟研究
应用CAFE法对6.5%Si高硅钢铸锭凝固组织进行了模拟研究,确定出了适合高硅钢组织模拟的模型。进一步用该模型研究了过热度及冷却条件对凝固组织的影响,结果表明,随着过热度的降低,凝固组织中柱状晶比例和晶粒平均面积均减小。水冷条件下,高硅钢铸锭凝固组织几乎全是柱状晶,而且晶粒粗大。空冷条件下,等轴晶区扩大,但柱状晶仍占主要部分。缓冷条件下,等轴晶区占主要部分,晶粒平均面积和空冷条件下相当。 The solidification structure of 6. 5% Si steel ingot was simulated based on CAFE method and the model suitable for simulating the structure of high silicon steel wad ascertained. The influence of superheat and cooling condition on the solidification structure were studied. It was shown that with the superheat decreasing,the proportion of columnar crystals decrease,and the average grain size become smaller. Under water cooling condition,the solidification structure of casting was composed of almo...
CN202121011955.9一种用于硅钢绝缘涂料混料装置
本实用新型涉及硅钢绝缘涂料技术领域,尤其为一种用于硅钢绝缘涂料混料装置,包括底座和混料箱,所述底座的顶端固定连接有混料箱,所述混料箱的左端内侧螺旋连接有塞块,所述混料箱的左端固定连接有控制器,所述混料箱的顶端内侧设置有进液管,本实用新型中第二电机带动螺旋杆便捷转动,螺旋杆和壳体的转动连接和可靠贴合将料斗中的配料螺旋送入混料箱,第一电机通过第一转动杆和第二转动杆带动搅动杆对混料箱中的配料进行大幅度扰动混合,贴合过滤网的搅动杆不断推动过滤网上被过滤的大体积固体配料,将其粉碎使其便于溶于液体配料中,实现充分混合,通过透明拉板便捷观察混料箱内侧混料情况,实现混料的彻底性,增加装置的实用性。
高牌号无取向电工钢技术发展及应用
对高牌号无取向电工钢国内生产情况、工艺技术、产品性能及应用领域等进行了阐述,并探讨了高牌号无取向电工钢产品的发展趋势。 This paper introduces basic facts on the production status,process technology and products’ properties and their applications of non-oriented electrical steel with high grade at home,and then discusses the development trend on technology for producing the non-oriented electrical steel with high grade.
取向硅钢用特种氧化镁的应用研究
采用XRD、SEM和激光粒度仪等手段,观察并研究了不同特性氧化镁在硅钢表面形成硅酸镁底层形貌特点,并结合热力学和差热-失重分析了MgO-SiO2的反应机理。研究结果表明:粒度小,活性值高的特种氧化镁在高温退火过程中与基体表面氧化物生成的硅酸镁底层,界面中硅酸镁底层嵌入基体较多,表面致密,颗粒细小,有利于形成附着性能优良的硅酸镁底层。 Surface microstructure of Mg2SiO4 coatings formed on the surface of oriented silicon steel coated with different kinds of MgO was investigated by XRD and SEM.The reaction mechanism between MgO and SiO2 was analyzed by TG-DSC and thermodynamic calculation.Results revealed that when the MgO with finer microstructure size and higher activity is employed,a dense Mg2SiO4 layer with finer microstructure and good binding to the steel substrate can be obtained.The results are very helpful for the prepar...
CN202023009664.4一种优化取向硅钢底层质量的打孔隔板
本实用新型公开了一种优化取向硅钢底层质量的打孔隔板,包括取向硅钢底层和分隔板,所述取向硅钢底层的上方安装有分隔板,且分隔板的内部设置有通孔,所述通孔的下方安装有卡合板,且卡合板的下方安装有硅胶密封垫,所述分隔板的右侧安装有三脚架,且三脚架的右侧安装有螺钉,所述三脚架的左侧安装有螺母,且三脚架的下方安装有固定横杆,所述分隔板的上方安装有定位套筒,且定位套筒的内部设置有内螺纹,所述内螺纹的内部安装有定位横杆,且定位横杆的两侧设置有外螺纹。该种优化取向硅钢底层质量的打孔隔板中,通过设置的通孔,分隔板将取向硅钢底层分隔时,通过通孔可以将分隔连通,减少在使用时分隔板阻拦取向硅钢底层的磁感性能。
铬、锰及退火温度对无取向硅钢组织性能影响
为探究铬、锰元素及退火温度对高强无取向硅钢性能的影响规律,借助OM、SEM、EBSD与万能拉伸试验机等分析不同制造工艺下3组不同含量铬、锰元素的无取向硅钢热轧、常化及退火处理后组织与性能。结果表明,试验钢热轧后组织不均匀,心部为沿轧向分布纤维状组织,边部为少量再结晶晶粒,常化处理能显著改善热轧板组织均匀性,消除热轧板中心部位的纤维状组织。经冷轧及退火后得到多边形铁素体晶粒,其中960℃退火,晶粒尺寸偏大,有利织构{100}组分体积分数减少,不利织构{111}组分体积分数增加,成分为0.2Mn-1Cr的1号试验钢960℃退火后铁损最大,磁感强度偏小;成分为0.5Mn-1Cr的2号试验钢930℃退火后,磁性能与强度等综合性能最佳,工频铁损P1.5/50为2.41W/kg,高频铁损P1.0/400为17.36W/kg,磁感应强度B5 000为1.638T,抗拉强度为685MPa。 In order to study the effect of Cr,Mn and annealing temperature on the properties of high-strength non-oriented silicon steel,the microstructure and properties of three groups of non-oriented silicon steel with different Cr,Mn content under different manufacturing processes were analyzed by means of OM,SEM,EBSD and universal tensile tester.The results show that the structure of experimental steel is not uniform after hot rolling,and the core is distributed in fibrous structure along the rolling ...
硅钢高温退火环形炉炉壳制作与安装技术
硅钢高温退火环形炉炉壳制作与安装精度要求较高,施工时通过对壳体原材料矫正、炉壳板拼焊、下料切割、型钢骨架组装及焊接、骨架及炉壳板矫正、骨架与炉壳板组装及焊接、炉壳矫正、零配件装置、定位钻孔、报验检查、出厂、内侧板安装、外侧板安装、顶板安装等环节的工艺技术控制,能保质高效地完成硅钢高温退火环形炉炉壳制作与安装,为以后同类工程的施工提供可借鉴经验。 The required precision of manufacture and installation technique of the silicon steel high temperature annealing annular-furnace shell is high.During construction , manufacture and installation of the silicon steel high temperature annealing annular-furnace shell could be finished high efficiently through correcting the raw materials of shell , furnace shell plate welding , material cutting , steel frame assembly and welding , skeleton and shell plate correction , skeleton and furnace shell asse...
CN202122561833.3一种适用于自动线的硅钢叠装系数性能检测装置
本实用新型公开了一种适用于自动线的硅钢叠装系数性能检测装置,涉及实验仪器自动化技术领域,为解决机器人自动上样至叠装系数测量仪经常发生碰撞的问题;本实用新型包括框架、上压板、下压板、压紧驱动机构、高度探规和加载力值传感器,其中压紧驱动机构设置于框架上端,下压板固定于框架内的下端,上压板安装于下压板上方且与压紧驱动机构的输出端传动连接,加载力值传感器安装于上压板与压紧驱动机构的输出端之间,高度探规安装在上压板上,且探头向下伸出上压板下端面,框架为“C”字形一体式刚性结构,其设有上下两个水平板,以及位于一侧的竖直板;本实用新型能够避免机器人自动上样时碰撞到框架,以及下压时高度探规压到试样。
CN202121551781.5超薄硅钢铁芯卷绕张力控制装置和纠偏装置
本实用新型公开了超薄硅钢铁芯卷绕张力控制装置和纠偏装置,包括工作台、固定架和底座,工作台的顶部安装有固定架,所述工作台的底部设置有按压杆组件,所述按压杆组件的底部连接有底座,所述工作台顶部的前端和尾端均安装有固定板,所述固定板的内壁设置有收捆轴,所述工作台的顶部安装有滑轨板,且滑轨板位于固定板的内侧。本实用新型通过导向辊和衔接板的设置,工作人员在使用时,根据收捆轴上铁芯的缠绕位置,对两侧导向辊进行调节,从而通过导向辊的转动性对铁芯的活动起到定位作用,两侧导向辊的主要作用是起到带料输送出来时的导向作用,能够保证带料快速平稳的送料时不发生跑偏现象。
正火对双辊薄带连铸5.28%Si-1.11%Al无取向高硅钢磁性能的影响
采用双辊薄带连铸工艺试制了2.6 mm厚5.28%Si-1.11%Al高硅钢薄带,对比了1050℃×5 min正火及不正火铸带280℃冷轧至0.5 mm后,再经900~1100℃退火的磁性能。结果表明,高硅钢铸带显微组织为等轴晶组织,正火后铸带边部晶粒长大,中心层晶粒变化较小。成品中析出物主要为较粗大的AlN和AlN+MnS复合析出物,尺寸为0.5~2.5μm。与不正火试样相比,正火试样成品铁损大幅降低,磁感小幅下降;随退火温度的升高,两种工艺下铁损和磁感都是先降低后升高,在1050℃出现最低值。 2.6 mm thickness 5.28% Si-1.11% Al non-oriented high silicon steel was produced by twin roll thin strip casting.Magnetic property of the strip un-normalized and normalized at 1050 ℃×5 min was contrasted after cold rolled to 0.5 mm at 280 ℃ and 900-1100 ℃ final annealing.The results show that microstructure of the strip is equiaxed crystal.The surface grain is coarsened and the center layer grain has little change of the normalized strip.The main precipitates are AlN and MnS+AlN with 0.5-2.5 μm s...
常化和退火工艺对冷轧无取向硅钢高频磁性能和强度的影响
冷轧无取向硅钢(/%:0.003C,2.35Si,0.22Mn,0.011P,0.002S,0.36A1,0.003 0N)经890℃或940℃3 min常化的2.3 mm热轧板冷轧成0.35 mm薄板。研究了常化温度和800920℃3 min退火对该钢高频(400Hz)磁性能和抗拉强度的影响。结果表明,830920℃退火时高频铁损P10/400值最低,随退火温度增加,晶粒尺寸增大,钢的抗拉强度降低;该钢的最佳热处理工艺为常化温度940℃,退火温度830℃,其抗拉强度Rm、高频铁损P10/400和磁感应强度J50分别为565 MPa,21.5 W/kg和1.69 T。 The cold-rolled non-oriented silicon steel(/%:0.003C,2.35Si,0.22Mn,0.011P,0.002S,0.36A1,0.003 0N) is cold-rolled to 0.35 mm sheet from 2.3 mm hot-rolled plate normalized at 890 ℃ or 940℃ for 3 min.The effect of normalizing temperature and annealing process at 800 920 °C for 3 min on high frequency(400 Hz) magnetic properties and tensile strength of the steel has been tested and studied.Results show that with annealing at 830 920 ℃the high frequency iron loss value P10...

