所有分类
  • 所有分类
  • 未分类

通过对35W300高牌号0.35 mm冷轧无取向电工钢卷(/%:0.002C、2.71Si、0.22Mn、0.015P、0.003S、0.0020N、0.55Als)头、中、尾组织、织构及对应的磁性能的试验研究,发现因热轧时12 MPa高压水连续冷却造成接触轧辊的钢卷头、中、尾在不同温度下轧制,卷取后钢卷头部处于卷心、温度略高而冷却速度略低于钢卷尾部,致使钢卷纵向组织、织构不同,成品卷头、尾各250 m内磁感逐渐增加,铁损逐渐降低,250 m外至钢卷中部磁性能稳定。通过将热轧辊的冷却方式改为周期冷却和卷取后的层流冷却改为钢卷70 m后开始冷却,至钢卷尾部70 m前停止冷却的方式使得钢卷纵向铁损差异明显减小,磁感差异略有改善。 According to the test research on structure and texture of head,meddle and end of 35W300 high grade 0.35 mm cold rolled non-oriented electrical steel strip coil(/%:0.002C,2.71Si,0.22Mn,0.015P,0.003S,0.002 0 N,0.55Als) and corresponding magnetic properties,It is found that due to 12 MPa high pressure water continuous cooling the roller in hot rolling process led to head,middle and tail of strip rolling at different temperature and after coiling the head of strip coil being in center of coil led t... 
2013-05-28 175 5.8

对CSP流程生产的无取向电工钢M50W800不同尺寸样品的磁性能进行了测试和分析,结果表明:采用不同单片检测的磁性能结果与标准的Epstein方圈样品检测对比,存在明显的偏差;且同一尺寸的单片纵横向样品之间相比较,对应的磁性能差异性也较大。几种不同尺寸的单片样品,以320mm×30mm尺寸的纵横向平均值最接近标准Epstein方圈样的性能值,其铁损偏差最小。 The magnetic properties of M50W800 non-oriented electrical steel produced by CSP process were tested and analyzed with samples of different sizes,showing that significant deviation existed compared to that of Epstein square circle sample.In particular,obvious difference in magnetic properties also existed between longitudinal and transverse samples of the same size.For test samples of different sizes,the average magnetic properties of 320mm×30mm samples are the closest to that of Epstein square ... 
2013-01-28 164 5.8

利用场发射电镜及能谱仪研究了取向电工钢薄、厚板坯铸锭中不同区域的析出相差异,确定了MnS、AlN及Fe3C的析出顺序和形貌特征。结果表明AlN以先析出的MnS为形核核心,形成粗大微米级的复合析出相。针状Fe3C既可以在复合析出相表面形成也可以在基体中单独出现,主要受冷却速度的影响。在1250℃保温1~2 h,AlN、Fe3C均可完全回溶,但部分MnS仍不回溶。MnS尺寸随着保温时间延长而增大。导致热轧板中沿轧向分布的粗大MnS,减弱了粒子钉扎力。 Precipitates in thin and thick slabs of electrical silicon steel were investigated by means of field emission SEM and EDS analysis.The precipitation sequence and the morphology of MnS,AlN and Fe3C particles were identified.AlN particles are observed to be nucleated on surface of MnS forming micron-meter-sized complex particles.Acicular Fe3C can precipitate on surface of the complex MnS/AlN particles or directly from matrix depending on cooling rate of the slabs.After holding at 1250 ℃ for 1-2 h,... 
2011-08-28 159 5.8

本发明公开了一种宽频率低铁损变频电机用无取向电工钢及制造方法,属于无取向电工钢领域。针对现有无取向钢在较宽频率范围内电磁性较差的问题,本发明提供一种宽频率低铁损变频电机用无取向电工钢,包括如下重量百分比的各组分:Si:2.80%~3.50%;Als:0.20%~0.60%;Mn:0.20%~0.60%;P:0.01%~0.20%;C:≤0.005%;S:≤0.02%;N:≤0.02%;Ti:≤0.005%;其余为铁和不可避免的杂质;其中C、S、N和Ti的重量百分比满足下式:C%+S%+N%+Ti%≤0.009%。通过控制合金元素的含量达到电工钢电阻率增加、磁滞伸缩减小,涡流和磁滞损耗均降低的目的。通过本发明提供的制造方法在正火过程中选用低温工艺,改善随着合金元素量的增加金属强度增加、塑性降低、冷加工性能降低的问题,使其最终在较宽频率范围内电磁性能优异。
2021-03-29 162 6.8

【作者】 朱凤泉; 黄生银; ...
2013-01-28 171 5.8

本发明涉及无取向硅钢技术领域,尤其涉及一种改善高牌号无取向硅钢冷轧断带的控制方法。按重量百分比计:[Si+Al]≥4.0%;Mn、S含量满足:S≤0.0015,[Mn]/[S]:200~400;1)热轧过程中使用保温罩,热轧轧制时投入边部加热,头尾100米内卷曲温度提高15~30℃;2)常化机组圆盘剪进行边部剪边前增加加热装置,剪切后增加毛刺打磨装置,采用煤气明火加热,保证钢板温度在韧脆转变温度以上;3)圆盘剪间隙满足关系式:ds=(0.15~0.45)d0ds:圆盘剪间隙,μm;d0:常化板板厚,mm;4)常化采用快速加热,控制钢带的预热段升温速度320~380℃/min,机组速度20~30m/min;5)常化工艺后,控制边部小于20μm的晶粒占比在5%以内。有效的减少了冷轧断带的发生,提高成材率1.30%以上,降低了生产成本。
2021-09-13 176 6.8

本文以热轧常化板为初始材料,采用二次冷轧法与三次冷轧法制备了0.1 mm厚的取向硅钢薄带,测定相应的磁性能,并通过EBSD取向成像技术检测了二次冷轧法与三次冷轧法各工艺过程中织构与组织演变规律。结果表明,采用最终冷轧压下率适中的三次冷轧法,能在冷轧至0.1 mm时保存较多的高斯晶核,使得高温退火后的磁性能明显优于二次冷轧法。最终冷轧压下率通过影响脱碳退火后样品中的{111}<112>织构组分及Goss晶粒数量对最终二次再结晶产生重要影响。 Grain-oriented silicon steel sheets with a thickness of 0. 1 mm were produced from hot-rolled and normalized sheets by two-step-rolling and three-step-rolling methods. Their magnetic properties were measured,and the textures were detected by EBSD technique. The results show that the three-step-rolling method,which has a moderate reduction rate of final cold rolling,can maintain more { 110} < 001 >nucleus,and thus obtaining better magnetic properties compared with the two-step-method. The f... 
2013-04-28 157 5.8

对应用动态加热进行短时温度退火的取向电工钢进行了二次再结晶研究。所进行研究的实验用取向电工钢是经过终冷轧和后续罩式退火后的一条工业化生产线生产的。研究结果表明,运用短时热处理条件可引起研究钢完全的异常晶粒长大。在实验室处理的材料的织构和金相组织与工业化生产的经过终退火而获得的相同的取向电工钢类似。但是,在实验室处理的取向电工钢的二次再结晶的矩阵中可观测到\"寄生\"晶粒。从磁性观点看,这些\"寄生\"晶粒含有不理想的{111}取向织构。 The present study was made to investigate secondary recrystallization in grain-oriented steels annealed at short time temperature exposures with application of dynamical heating.The investigated GO(Grain Oriented) steels for experiments were taken from one industrial line after final cold rolling reduction and subsequent box annealing.It was shown that application of short time heat treatment conditions could lead to complete abnormal grain growth in the investigated GO steel.The texture and mic... 
2011-04-28 162 5.8

本发明公开了一种宽频率低铁损无取向电工钢及其制备方法,属于无取向电工钢生产制造技术领域。它从电工钢表面向内依次包括0.005mm~0.1mm的渗透层和钢材内芯;所述渗透层是由硅原子向电工钢内渗透形成,渗透层中的硅元素含量为3wt%~8wt%;所述钢材内芯包括2.0wt%~5.5wt%的硅元素和不少于93.2wt%的铁元素。本发明能保证无取向电工钢具有低频低铁损性能同时有效降低高频条件下的铁损,具体铁损性能为:铁损P1.5/50≤2.35W/kg,铁损P1.0/400≤13.8W/kg。
2021-11-09 165 6.8

本发明涉及一种冷连轧法生产无取向高硅钢的方法,RH真空脱碳处理后,铝脱氧及部分铝合金化,合金化后大罐钢水净循环大于3次或大于5分钟;熔炼合格钢水至连铸开浇前静置时间大于二十分钟;控制过热度5~15℃;采用电磁搅拌,控制等轴晶比例45%以上;3)热轧工序板坯装炉温度大于750℃;常化使晶粒尺寸在90~110μm范围内;连续退火炉加热段温度设定950~1150℃,均热段温度设定900~1050℃,全氮气干气氛保护,控制晶粒尺寸120~170μm。生产全过程中的热履历参数控制,充分发挥设计的微合金元素功能,改变析出物的组成、大小、形态及分布。
2021-08-19 168 6.8

研究了采用高温卷取热轧态原料和常化态原料生产高牌号冷轧无取向电工钢组织、织构和磁性能。研究发现钢卷采用750℃高温卷取,下线后立即采用\"保温罩\"对钢卷进行保温,时间96h,然后空冷至100℃时上线生产的工艺可取代常化工艺生产高牌号冷轧无取向电工钢。冷轧上线前,热轧态原料的表层为大量的再结晶组织,这部分组织包括了热轧轧制时保留下来的动态再结晶组织,钢卷本身高温回复后产生再结晶晶粒,以及在保温罩内保温时形成的再结晶组织。高温卷取的热轧态和常化态的热轧卷作为原料时,试样织构类型相似,取向分布密度接近,再结晶后织构类型仍然相似,取向分布密度仍然接近。Goss织构对磁性能增加有促进作用。实验钢中较好的磁性能对应的织构[{100}+Goss]/{111}的比值较高,体现了织构的遗传性。 Microstructure,texture and magnetic properties of high grade cold rolled nonoriented electrical steel which made of hot rolled material with high temperature coiling and with normalization were studied.Steels coiled in high temperature(at 750 ℃),stacked with insulation cover for 96hand air cooled to 100 ℃ were using to manufacture high grade nonoriented electrical steel.The process can replace the normalization process.There are a lot of recrystallized grains in the surface layer of the coil wit... 
2014-03-28 162 5.8

为开发高效电机用冷轧无取向电工钢,借助实验室薄板坯连铸连轧模拟设备及扫描电镜、透射电镜等检验手段研究了成分、组织、织构和析出物等对无取向电工钢磁性能的影响规律;结果表明:常化处理使组织均匀化并增加有利于磁性提高的织构组分;采用CSP流程开发的高效电机用无取向电工钢铁损平均值3.4 0 W/kg,磁感≥1.68 T。 In order to develop electrical steel for high efficiency motor,effect of components,microstructure,texture and precipitation on magnetic property of electrical steel are analyzed.From the result,normalizing treatment makes microstructure uniform and increases component of favorable texture.Iron loss of electrical steel developed by CSP line is 3.40W/kg and magnetic induction is more than 1.68T. 
2011-01-28 192 5.8

站点公告

网站试运行,请大家关注本站公众号,多提宝贵意见!

显示验证码
没有账号?注册  忘记密码?